Viking 6030 sewing machine rebuild

A very nice lady gave me a Viking 6030 sewing machine (as well as this serger).

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It had what is said to be a typical problem for this make and model:  the lubricating oil had solidified into a wax- or plastic-like consistency, and the upper main shaft, many of the controls, and other mechanisms were frozen.  The only way to repair this is to completely disassemble the machine, clean out the old oil, and reassemble it with new oil.  After such a complete rebuild, all of the normal service adjustments must be made.

This post documents the rebuild process with photos and provides documentation.  When done, your machine may be able to do this:

30.0.  All done!

I took on this project because I have always wanted to add a sewing machine to my tool collection, because it is related to my hobby of fixing cars, appliances and other machines, and because I knew the sewing machine would be a very complex mechanism and it would be fun to ’solve’ such a puzzle.  When it was given to me, I did not expect that its problem would require complete disassembly of the entire machine, but it turned out a welcome challenge.

If you are not mechanically inclined, or are doing this to save money, I do not recommend doing it yourself.  Screw slots are easy to strip, even with my life-saving screwdrivers, and removing stuck screws takes both strength and finesse.  There are about 350 parts in this machine, and it can be tough to figure out how they fit together.  The mechanisms are very complex, and they must be understood to really get them working properly.  While researching the machine, I found a highly-rated seller on ebay who periodically makes a listing to perform exactly this procedure for an extremely reasonable $258 + shipping, a great price for a rebuilt example with all the cams and accessories.  I have no idea how he can do this quickly enough to make it worth his time, but judging by his consistent 5-star feedback and raving comments, he cuts no corners, and I am very impressed.

If there’s anyone who’s made it this far and still wants to do the job, I would really love a post in the comments section!  I wish you good luck, and let me know if you have any questions.

Preparation

A minimal set of tools is needed.  Without this Chapman screwdriver set, which has 12 bits for slotted heads of varying widths and thicknesses that fit any slotted head perfectly, I would have been suffering with stripped slots.  Also needed are a standard set of feeler gauges, circlip pliers, and assorted pipe brushes, all available for cheap from Harbor Freight.  Others are standard:  nut drivers, pliers, a knife, scissors, a metric ruler, flashlights.  For cleaning, kerosene seems to be the recommended solvent for the hardened oil; a paint roller pan with the pipe and other brushes and some large blank white paper to place parts to dry complete the kit.  For disassembly, have several dozen ziplock bags of various sizes to keep parts organized.  Finally, have a digital camera with a macro mode.

9.0.  Tools used

Disassembling and cleaning

The service manual (see link below) contains instructions for dismantling some parts.  Take plenty of close-up pictures so you can both remember the order of how things were dismantled, as well as how things fit together.  As you take things apart, put related parts in ziplock bags.  This machine has about 350 parts, and it is very difficult to keep track of all of them, so use small bags for screws, and put those together with the related larger parts into medium bags, and then put those bags into large bags.  The more organized you are, the easier this job will be.  I did a pretty good job, but came out with this one extra part (I’ll paypal the first person to correctly identify it $5), so be organized!

9.1.  Left over washer

Kerosene can loosen up the hardened grease.  It is a good idea to take off the covers and applyto the whole inside liberally, allowing to soak for a couple of days with periodic reapplications.  Pay particular attention to the upper and lower shafts, which can freeze in their bushings, and the various gears that are mounted on the shafts.

When cleaning, put kerosene into the paint roller pan, and scrub the parts with brushes.  Use pipe brushes to clean all holes.  Arrange parts on a big piece of white paper to dry, grouped together as they were in the bags.  When the kerosene gets too dirty, pour it in a jar and allow the dirt to settle overnight; pour the kerosene back into the pan, leaving the sediment behind, to use again.  Kerosene dries slowly, and the parts will need to sit for at least 24 hours.  There should be no traffic in the area so that parts are not disturbed and disappear.  When dry, repack into their baggies for assembly.

Disassembly took me about two days, and cleaning another two days.  Order is the reverse of assembly, so follow the Assembly gallery pictures backwards.

Pics of the parts drying at the ends of day 1 and day 2.  These are all the parts in the machine!

9.2.  All parts #1

9.3.  All parts #2

Assembly

When putting the parts back together, be sure to understand how each part works, and test each part of its motion.  This can take quite a bit of time, but will reduce later problems, and when there is a problem, you will be better equipped to diagnose and correct it.  Do not rush, take your time.  If you get frustrated, take a break and come back later.

After some online research, it seems that the most recommended grease is Tri-Flow lubricant with teflon.  Initially, I used the grease, but I believe that it slowed down the fast-spinning parts and bogs down the motor. Since then, I have been told by two experts to use the thin lubricant, at least in the sintered bushings.  In general, any two parts that move against each other should be lubricated.  Apply lubricant or grease to both contact surfaces.  When using grease, after fitting the parts together, if extra grease has not already squeezed out, a small amount can be added to ensure the joint will not starve of grease.  Do not overdo it though, since too much grease will just make a mess.

Assembly is detailed in the gallery below.  The pictures are annotated.

Adjustment

The pictures in the below gallery follow most of the adjustments in the manual.  They are annotated, and may contain hints when the manual is unclear, or requires a tool that us amateurs don’t have.

One adjustment to note is the shuttle cover clearance.  The manual calls for a special gauge.  The same gauge is used on the flat-bed models, so the clearance must be the same.  On the flat-bed models, one of the diagrams shows the gap between the actual shuttle and the back of the shuttle cover as 0.4mm.  I found that parts of the rim of the shuttle and the entire back of the shuttle cover are flat, so it is possible to use normal automotive feeler gauges for this adjustment.  See the adjustment described in picture 19.15.  I have no skipped stitches and the machine doesn’t jam, but it sounds quite loose and makes noise.  If anyone measures this gap before disassembling their machine, I’d very much like to know the measured gap.

Documentation and links

Factory service manual Read it!

Chapman screwdriver set Life-(or at least project-)saving screwdrivers

Viking mechanic on ebay My latest idol

Tri-Flow Lubricant Aerosol $14 shipped on ebay

Pre-1980 Viking Sewing Machines Yahoo Group run by Bill Holman

Final notes

For most of this project, I drew from my considerable experience as a shadetree mechanic.  I read very little of the service manual before doing this, so my process may have significantly deviated from the manual’s.  Please post a comment if I did anything that looks troublesome so I can correct my documentation for the next reader.

Thanks for reading, and thanks for all corrections, comments, and since I can’t imagine there are any others in the world who might be interested in this topic, I appreciate readers just saying hi in the comments.

Before undertaking this project yourself, be sure that you understand the complexity of this task.  Don’t hold me accountable for the failure (or even success) of your project!

Update

The Viking guru from ebay, linked above, wrote me these nice comments.

First message:

Hi, betelnut. Looks like your leftover washer might be the special one that
goes between the long screw that you put in against the long spring, and
the piece that moves the cam in and out when you turn the stitch selector
knob. Quite a project to undertake without training in all the tricks that
lurk in these machines! You must have a very thorough general mechanical
knowledge. I had never thought of using regular feeler guages to set the
hook cover clearance- could be done if one is fussy enough! The most
critical part is the two posts opposite each other must be exactly the
same; after that is accomplished, you can adjust the third post while
running the machine (with no needle mounted) to get the least noise. Most
of the machines I see have the hook-needle clearance set wrong because the
last person to work on it assumed the running alignment of the hook is
determined by the hook DRIVER- but actually when running it is against the
hook COVER. So they set it statically with the hook just missing the needle
while resting against the hook driver. The Viking gauge that you put in
place of the needle, a thing slightly fatter than a needle, allows you to
set the clearance statically so that it comes out right when the machine is
running. I don't know how you might do this without the guage except by cut
and try. I'll get back to you with another message, I have to go now... 

Regards, Chris

Second message; NOTE: SEE UPDATE 2 BELOW ABOUT WHY NOT TO USE WD-40:

Not wishing to spend my days standing over a pan of kerosene, I usually
clean the hardened grease off parts by physically scraping it off, and
wiping and or scrubbing with WD40, then drop them in a closed container of
rubbing alcohol. Let dry, the remainder is a powdery white stuff that I
clean off with a wire wheel on a bench motor. I poke pieces of WD40
soaked rag through holes and follow with clean rag. There ARE of course more
drastic and toxic chemicals to use when things are stuck so bad I can't get
them apart with WD40. I don't usually remove the top shaft unless
it is stiff turning, as sometimes happens when the machine has been treated by
someone just spraying solvent into it- this melts the grease which then
spreads into everything and re-hardens into a gluey consistency and makes
everything more difficult. I wish I knew more about what various chemicals
do to the sintered oil-impregnated main topshaft bearings- I try to stay
away from them with chemicals unless absolutely necessary to get it apart.
I have seen that some people drill oil holes into the top of the machine,
like the early 6000's had, so the user can oil the topshaft bearings; I
haven't had to do that yet. I have just made sure the bearings were well
oiled with regular sewing machine oil when I reassemble- haven't had any
stiffen up again that I know of. For lube when reassembling, I use the
liquid Tri-flow (not grease) which Viking recommended at seminars back when
they were still concerning themselves with these models. Before they
discovered Tri-flow, they recommended reassembling completely dry, no lube
at all.  (the hardening-grease problem had started showing up on the early
6000's while the later ones were still being sold, and they were of course
quite concerned about it) One place I do use a dab of grease, is on the
bobbincase spindle, which if left dry will sometimes develop a harmonic
vibration of the bobbincase that makes a screeching noise. About to run out
of room- 1 more messg.

Third message:

Thank goodness ebay now lets you reply more than once to a "question".
Reviewing my first message, I thought I should make clear, about the
needle/hook clearance and hook driver/hook cover clearance- you FIRST have
to set the needle in the right place in the needleplate; then set the
hook/needle clearance, THEN the hook cover clearance. When you are done,
observe the hook/needle clearance while holding the hook OUT against the
hook cover; it should be as close as possible without actually touching. If
it's not good, you will have to move the hook DRIVER and then re-adjust the
hook cover clearance also. (in models after the 6000 series, Viking made
all this much simpler. The hook cover screws directly to the casting, so
the cover clearance is fixed, no posts; the needle bar frame is moved to
adjust hook/needle clearance, and the needle PLATE can be moved slightly
front-to-back with an eccentric stud. Well... Much of this may have been no
news to you, who seem so very mechanically skilled; but I was so impressed
by your adventurous rebuild, I wanted to see if I could offer you something
helpful. Regards, Chris

Finally, in answer to some other question I’ve now lost track of:

The hook driver can also be moved in and out by loosening the set screw
from the bottom, moving the whole driver/bearing/gear assembly, but then of
course you have to reset the gear mesh by moving the meshing bevel. You
want just a tiny bit of play so there's no bind. The buttonhole cutting
space can be adjusted, it's on page 121 if your book is the same as mine.
If your book doesn't have it, I can try to describe it. Dry assembly-
refers to the mechanisms moved by the knobs, and the needle movement
sideways, the fabric feed, and the gears. The running bearings such as top
and bottom shaft bearings do need oil. The later models with "permanantly
lubricated" bearings there, and no oil holes, I have sometimes seen
stiffened up, but I'm not sure whether the "permanant" oil supply actually
ran out, or if it was the result of some chemical contamination, or perhaps
just a long period of disuse.

Update 2

Thanks to Page who left a comment below, I became aware of a Yahoo Group dedicated to pre-1980 Viking sewing machines. The group was founded and is moderated by Bill Holman, a well-known authority on these machines in online sewing machine circles, and who is extremely generous about sharing his knowledge. Because of my mention of WD-40, which unbeknownst to me can kill the Viking sintered bushings, my membership request to the group was rejected, with the following information about why that mention should be (and has been from my own write-up!) removed:

Your blog has been previously brought to my attention, and while I admire your initiative,
I am appalled by your suggestion of using WD-40 in these old Vikings. I have been a
Viking-Husqvarna technician for almost 50 years, and that stuff is a terrible choice for
any of the machines, and the kiss of death for a sintered bushing. Within months of the
introduction of the 6030 in 1972, Viking sent out a warning to never use WD-40 in their
machines, because it will leave a residue in the pores of the bushings that prevent
the oil from exiting, or the bushings from soaking up any additional oil that is externally
applied.

This is not a matter for discussion. It is a fact, and it should never be used. On other
mechanisms, WD-40 dries leaving a sticky residue that has to be washed off. It has contributed
to pattern mechanisms and buttonholers locking up, and needle bar frames refusing to swing.
WD-40 was designed as a water displacement solvent, and that is all it is good for. It
should not be used on anything more precise than a garage door hinge. If precision
equipment needs to be freed up, there are many products that will do as good a job as
WD-40, without the drawbacks. Even kerosene is safer as a solvent, and CRC 5-56 is
excellent. The best possible product is Triflow. It is somewhat of a penetrant, and a
great lubricant.

Thanks, Bill! I had to leave the WD-40 references where they were quoted in the first Update section, but hopefully the big warning message pointing to this update will ensure that readers are informed.

16 Responses to “Viking 6030 sewing machine rebuild”

  1. Anne Says:

    Hi!

    Awesome job, and I don’t use that word lightly.

  2. Yammy Says:

    Very organized!!! Well done! Well written too!

  3. Cordelia Says:

    Amazing. It would have made a good movie. The stitch sampler is cool. I like the treatment of the sewing machine as a tool. It sounds so much more substantial, that way.

  4. Jon G Says:

    Wow! This is fantastic! The 6030 is the same machine my wife has which she inherited from my grandmother. It recently froze up and needs the same overhaul you just performed. Your work is a huge confidence boost as I am planning on doing the job myself. Thanks.

  5. jman Says:

    Great to hear Jon, good luck! It’s a lot of work, but worth it. If you get stuck, let me know, I’ll try to help. Also, if you figure out where my mystery washer goes, let me know!

  6. Page Says:

    A very nice lady gave a sewing machine to a very nice man who gave it to his very nice wife (she’s got to be nice after that effort!). This is fantastic and thank you SEW much for sharing the Viking Technical manual. I have to try to reset the hook in the machine I bought on CL. I hope I can do it as a very nice lady sold me a 60 40 for a very nice price for me to give to my very nice girls who like to sew very nice things (:

  7. jman Says:

    Page,

    Thanks for the message, I hope these instructions help. Your post got me off my lazy butt, and I finally posted some messages from the Viking Guru that might help you with the hook alignment. In fact, I just recently went back and fixed mine; my original job was close but wrong, and I broke a needle. Good luck!

  8. Laura H. Says:

    What a saga. :) I was just looking for some documentation on my 6030 (paper gets so lost over the years) and happened on it.

    It’s a great machine, well worth the effort to get it working. Mine has never frozen up; I guess I’ve been lucky, because I have laid off sewing for up to several years at a time. I have cheated now and then, and lubricated it.

  9. russ Says:

    JMan, I have been interested in tractors for the last few years and have a lathe and mill. It sure seems to be good for a persons mind to work a good puzzle.

    I got a frozen stuck 6030 yesterday, could be a lot of fun. Your time and willingness to share your adventure earns you a gold star, as my grandmother used to promise.

    Nice service you have done for all who wish to preserve this great machine. -russ

    Seriously kudos!! -russ

  10. jman Says:

    Laura, hope the documentation here helps. I think I have a scan of my Viking user manual; let me know if you need it.

    Russ, great machines! The service manual p. 7 says the manufacture of the shuttle and bobbin each require about 150 operations to complete. I’m pretty sure I didn’t get an original Husqvarna bobbin with mine, but you can tell the shuttle is not a simple hunk of metal!

  11. Crystal Says:

    I just got a 6440 free off craigslist that runs, but slow. A repair shop had “cleaned and oiled” it, but from looking at the insides of it, it doesn’t look like they did anything. It’s really gummed up in a few places.

    I’m so glad I found this. I hope it will help me get this machine running.
    I’m so excited. :)

  12. jman Says:

    Hi Crystal, lucky you! Slow is good: it means everything’s there.

    Don’t take the machine completely apart like I did, unless you’re crazy (like I am). Just get some aerosol Tri-Flow and squirt it in around the bushings of both shafts and other moving parts. Hopefully the kerosene solvent in the Tri-Flow will help dissolve the gum, and the Teflon will help lubricate, and you’ll be running again with very little trouble!

    Please post back and let us know how it goes. Good luck!

  13. cindy Says:

    I got a 6030 free on CL, straight stich runs fine…the reverse button does not return to allow the forward stitching to resume…any ideas?

  14. jman Says:

    Hi Cindy,

    I’d do the same thing I mentioned above: squirt some kerosene in there and leave it for a couple of days, work the mechanisms occasionally and squirt a litlte more, and then spray Tri-Flow in there. Your Viking certainly has the same problems as the rest of ours: the old oil became gummy over time and is making the mechanisms sticky.

    Good luck, and post back your results!

  15. Cindy Says:

    I used the triflow….it is slowly getting better…I still can not use the cams because a soon as it goes into reverse it stays in reverse and doesnt return to forward , now, since a couple days of triflow…it seems to slowly be returning….patience and triflow seem to be the fix….thanks for your help.

  16. russ Says:

    Jman,

    After unstucking and a new take up slide, my machine 6030 has been functioning very well. I get an extra wrap around the bobbin about 20% of the time. It doesn’t cause any stitch problems and I can’t even tell till I pull the piece from the throat and see the extra thread. Not a big problem and seems to be related to the quality of the bobbin wind and probably the thread too, as I am using serger thread.

    Sewing is not easy. Seems pretty fun though. I made curtains and a couple pairs of slippers so far. There are some good resources around for pattern design. I will try making a shirt(s) similar to the Bowling Shirts as worn by Charlie Sheen (Harper) of 2.5 men.

    Thanks again for hosting this great resource.

    Kind regards to all, russ

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